Fixed compile error when QUICK_HOME is defined.
As well a couple of minor changes to handling of extruder offset for dual x-carriage mode.
This commit is contained in:
		| @@ -696,7 +696,7 @@ static float x_home_pos(int extruder) { | ||||
|     // second X-carriage offset when homed - otherwise X2_HOME_POS is used. | ||||
|     // This allow soft recalibration of the second extruder offset position without firmware reflash  | ||||
|     // (through the M218 command). | ||||
|     return (extruder_offset[X_AXIS][1] != 0) ? extruder_offset[X_AXIS][1] : X2_HOME_POS; | ||||
|     return (extruder_offset[X_AXIS][1] > 0) ? extruder_offset[X_AXIS][1] : X2_HOME_POS; | ||||
| } | ||||
|  | ||||
| static int x_home_dir(int extruder) { | ||||
| @@ -711,7 +711,7 @@ static void axis_is_at_home(int axis) { | ||||
|   if (axis == X_AXIS && active_extruder != 0) { | ||||
|     current_position[X_AXIS] = x_home_pos(active_extruder); | ||||
|     min_pos[X_AXIS] =          X2_MIN_POS; | ||||
|     max_pos[X_AXIS] =          X2_MAX_POS; | ||||
|     max_pos[X_AXIS] =          max(extruder_offset[X_AXIS][1], X2_MAX_POS); | ||||
|     return; | ||||
|   } | ||||
| #endif   | ||||
| @@ -907,7 +907,7 @@ void process_commands() | ||||
|       { | ||||
|         current_position[X_AXIS] = 0;current_position[Y_AXIS] = 0; | ||||
|  | ||||
|        #ifdef DUAL_X_CARRIAGE | ||||
|        #ifndef DUAL_X_CARRIAGE | ||||
|         int x_axis_home_dir = home_dir(X_AXIS); | ||||
|        #else | ||||
|         int x_axis_home_dir = x_home_dir(active_extruder); | ||||
|   | ||||
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